Did no one read MY message? Jamie wrote me up a synopsis of the event and the car.
Spoiler alert: After all of this transpired, he worked on the car a few days after the event. There was gas. Just not enough to warrant the car actually moving under any speed. He's not sure where all the gas went, but it wasn't in the tank.
Jamie's words:
Sunday - Dixie AutoX - 48 degrees F and damp
Took the Slotus out for a day of adventure, not really sure of what was going to happen. It was 48 degrees and wet. There were places on course that held water all day. The turn out was rather low considering the next event is an SCCA National Tour.
We warmed the car longer than usual due to the outside temperature. Tires were set a little higher trying to get as much temperature in them as possible.
The Slotus performed well except the carburetor did not like the cool weather at all. Once the car got going, all went well during the morning session. We are still working on the chassis setup since the addition of the wing. As confidence increases, the speed keeps going up. A big relief to all involved.
Everything went very well until the last runs and we started losing power. After a short deliberation, we found out there is a fuel pickup problem in the fuel cell. [Not, just lack of fuel, period.]
Before the next event we, meaning Earl, is going to replace the pick up hose in the cell. [Nope, just gonna add gas.] The other problem that showed up was the steering quickner unit is beginning to seize up. Plans are in the works to eliminate that because the power steering rack is faster rater so the quickner isn't needed as much. [Note: JD never intended to add power steering. He did it for me. The quickner was supposed to help him without power steering. So I'm pretty sure I caused the issue there.]
All should be ready for the next event in March as we continue to add to the Slotus story. So stay tuned in when HamDip says, "Is it OK to see the front tires smoke too?"